Another thing to happen at around the same time, was after driving the car, I heard a hissing sound from the engine bay, which was coolant spraying from one of the radiator hoses. After it cooled down, I saw why - when the AFM had been moved (for the custom intake pipe and K&N air filter) an old bracket had been left on and was rubbing
So I removed the bracket and replaced the hose, also the other hose that comes from the top of the radiator had the blow off valve rubbing up against it, and felt very weak in that place, so I replaced that hose too. To save the damage happening again I went for a smaller (and much better anyway) BOV, a Turbosmart Vee Port
Mounted it using some hosing, to angle it for more space.
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